bobhaha
0
- Joined
- May 31, 2009
- Messages
- 3,239
- Points
- 63
Hey guys!
I've acquired a vintage (probably around 25 year old) variac from a good friend of mine. He worked as an electrical engineer for many years and has an enormous assortment of different test gear and equipment he has acquired over the years. Anyway... One day I was over at his house and told him that I was looking for a variac and low and behold... he said he had a spare one that needed work. I hesitantly took it off him knowing these are pretty expensive; so I promised that I would make it all pretty and give it a good home.
So this is what I got from him...
Notice the extreme angle of the top plate... Carbon brushes are not touching and there is no end stop.
It's an Australian made variac, made by Warburton Frank
It's an 8 Amp rated variac built for 240V 50Hz input.
So the first thing I did was take the top plate off and unscrewed the middle plastic insert. It was apparent that this variac has seen some use, but the windings looked great! No signs of over heating or arcing! I was really happy :drool:
The copper contacts are quite oxidized and full of muck... So I got to work cleaning it with a tiny bit of isopropyl alcohol and a rag.
I then used some 1000 Grit wet and dry sand paper and carefully went around sanding down to the clean copper surface. I then polished it up with 1200 Grit sandpaper just to make it look pretty
You can see the state of the contacts before on the right and after on the left.
Next thing to fix was the base... It was pitted and oxidized and didn't particularly look good.
I gave it a quick sanding with 1000 Grit sandpaper...
Then a little wash with isopropyl alcohol and a rag.
The next thing to do was fix this badly aligned top plate...
I placed the assembly into the vice and decompressed it inorder to remove the circlip.
I replaced it with a stronger clip then removed it from the vice...
It helped, but didn't fix the problem... Still no endstop and it still sat kinda wonky..
So I placed a washer to the outside edge, removed all spacers on the inside edge and replaced the circlip...
And that worked great!!
In this picture the plate looks crook because there is no shaft running through the middle and the brushes springs are pushing one side up. But it's atleast touching the contacts now
I placed a test shaft to see what it looks like...
Looks great! Now there is pressure on the contact and it glides soooo smoothly! I'm really happy!
Here is a short video showing it all working together....
Next step is to measure up and get a custom lasercut case for it. I'm hoping to do it all in acrylic so you can see inside. I also need to find a sturdy fibreglass rod to replace the aluminium one I have in there right now. Then lastly I need a voltage scale and knob made up... Those will probably be laser cut/etched as well.
So stay tuned for more!
-Adrian
I've acquired a vintage (probably around 25 year old) variac from a good friend of mine. He worked as an electrical engineer for many years and has an enormous assortment of different test gear and equipment he has acquired over the years. Anyway... One day I was over at his house and told him that I was looking for a variac and low and behold... he said he had a spare one that needed work. I hesitantly took it off him knowing these are pretty expensive; so I promised that I would make it all pretty and give it a good home.
So this is what I got from him...
Notice the extreme angle of the top plate... Carbon brushes are not touching and there is no end stop.
It's an Australian made variac, made by Warburton Frank
It's an 8 Amp rated variac built for 240V 50Hz input.
So the first thing I did was take the top plate off and unscrewed the middle plastic insert. It was apparent that this variac has seen some use, but the windings looked great! No signs of over heating or arcing! I was really happy :drool:
The copper contacts are quite oxidized and full of muck... So I got to work cleaning it with a tiny bit of isopropyl alcohol and a rag.
I then used some 1000 Grit wet and dry sand paper and carefully went around sanding down to the clean copper surface. I then polished it up with 1200 Grit sandpaper just to make it look pretty
You can see the state of the contacts before on the right and after on the left.
Next thing to fix was the base... It was pitted and oxidized and didn't particularly look good.
I gave it a quick sanding with 1000 Grit sandpaper...
Then a little wash with isopropyl alcohol and a rag.
The next thing to do was fix this badly aligned top plate...
I placed the assembly into the vice and decompressed it inorder to remove the circlip.
I replaced it with a stronger clip then removed it from the vice...
It helped, but didn't fix the problem... Still no endstop and it still sat kinda wonky..
So I placed a washer to the outside edge, removed all spacers on the inside edge and replaced the circlip...
And that worked great!!
In this picture the plate looks crook because there is no shaft running through the middle and the brushes springs are pushing one side up. But it's atleast touching the contacts now
I placed a test shaft to see what it looks like...
Looks great! Now there is pressure on the contact and it glides soooo smoothly! I'm really happy!
Here is a short video showing it all working together....
Next step is to measure up and get a custom lasercut case for it. I'm hoping to do it all in acrylic so you can see inside. I also need to find a sturdy fibreglass rod to replace the aluminium one I have in there right now. Then lastly I need a voltage scale and knob made up... Those will probably be laser cut/etched as well.
So stay tuned for more!
-Adrian
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